Rodgers' Piano Restorations
The Best Piano Rebuilding in the Business
9091 Ox Bow Rd.   North East, PA 16428
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Restoration of a Lester Upright for Mark Steele


Home Up

 

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1)  The piano before work began.  When we first scheduled this project, I had priced the work based upon doing a simple, cabinet grade finish.  However, when I saw the piano and how beautiful it was, I offered to throw in a grain filled, rubbed finish at no extra charge.  I simply couldn't stand to do less than the best for such a pretty piano.  Despite its present horrid condition, this piano has great bones.  It is my belief that, if we do a really thorough job on rebuilding it, this piano will be able to hold its own with any similar style of Steinway.  
2)  The back of the piano showing how dark the wood has become.  This discoloration speaks of years of exposure to moisture and also, probably, heat.
3)  When the lid was removed the condition of the pin block was revealed.  The wood has totally come unglued and the plate was bending forward.  This could have broken the plate but, happily, it didn't.  The repairs needed to set this right will be thrown in at no extra cost.  The customer is already considering the idea of doing more work than was originally intended.  I want to help make these additional, very important projects possible by throwing in as much free and/or low cost work as I can manage in order to enable the owner to be able to get the really important things done.

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4)  Now all the removable boards have been taken off the piano and their hardware removed.  They are now ready to go to the stripper to have their old varnish or shellac removed.  Even the keybed has been removed to make way for the restringing of the piano.  Now, the old strings are being taken off.   First the tension was removed from the strings because of the compromised pin block.  I wanted to get that string tension off as soon as possible.  Next, I will measure the wire sizes to discover the original scale.  If the scale is a good one, it will be reused.  Otherwise, it will be remade to a more modern design as needed.  The final decision on just how far we will go with restoration has yet to be made by the owner.  Budget is a concern which will have to be weighed against the piano's current condition and the owner's goals for the finished product.  It is already becoming apparent at this stage that the sound board is so badly damaged that it cannot be restored.  The bridges are also looking bad but I will wait until I have the strings all off so that I can examine the bridge pins and clean out the cracks before I make a final determination.  The news isn't all bad; even if we have to replace the sound board, action and/or bridges, the finished piano will far exceed anything that could be purchased new for the same amount of money.
5)  Recording the scale of the piano.  By checking the wire sizes used originally, I can determine if I can rescale the piano based upon the original scale; based upon the original with modifications; or if I have to rescale from scratch.   This piano may have to be done from scratch.  The original scale design was far from industry standards so I think I can really improve it.
6)
  The bottom board had been exposed to moisture just like the rest of the piano.  This board suffered quite badly from it causing it to come almost completely unglued.

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7)  Here, you see that the bottom board has been realigned and clamped up using fresh hide glue.  The old glue joint was done with hide glue so using fresh hide glue will ensure the best possible bond.  The new glue will actually serve to reactivate what is left of the old glue, thus bringing the old glue back into functionality as well.
8)  All the strings are now off the piano.
9)  Doing some measuring on the bass bridge.  This bridge is badly designed.   However, the plate is so nicely made that I have lots of room to make changes to this bass bridge in order to improve the scale dramatically.  For instance, the length of the shortest string on this bass bridge is easily 100mm longer than what you would find in a Steinway M grand piano.  This gives me lots of opportunity to improve over the original.  Since this original bass bridge has been so badly exposed to moisture, the wood is literally shredding.  It will be impossible to reuse this bridge.  As long as I have to make a new bridge, I'm going to go the extra mile and redesign the bridge to vastly improve the tone production.  (Provided, of course, that the owner gives me the permission I need to proceed.)  In this photo, I'm taking some preliminary measurements and marking the sound board to help me know what my "wiggle room" will be once the plate is out.

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10)  Removing the tuning pins.
11)  The plate screws have all been removed as have the action mounts and the nose bolts.  These are all kept in order by passing them through a piece of cardboard in the way they appear in the plate.  This arrangement is also useful when it comes time to clean and lacquer these.  The cardboard serves to hold them in place for me.
12)  The plate after it has been removed.  The fact that the pin block had come completely unglued could easily have broken the plate.  We're very lucky that this didn't happen.

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13)  The case with the plate out.  Also, the arms which hold the keybed in place have been removed as well.
14)  The pin block was totally unglued from the back of the piano.  All it took was the removal of a few screws that passed through the sound board into the bottom ledge of the block to have the block fall right out of the piano.  The fact that the block had done this, had also caused the sound board (which was glued to a rabbit placed at the bottom edge of the block) to break loose years ago.  This was the beginning of the end for this sound board.  The piano's condition as I took it apart in the shop clearly indicated that the sound board had totally died and could never be resurrected.   Unfortunately, the bridges are showing the same indications.
15)  A different angle photo to show that the sound board's upper edge is now totally floating in mid air now that the pin block has been removed.

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16)  Pulling the pins out of the bridges.  This is the best time to do this job.  These pins can be real knuckle busters if you leave them in.  Since they will need to come out in order to make a good pattern for replacement it is best to remove them now before they can accidentally cut me as I work with the board and bridges later.
17)  The outer case of the piano has now been scraped free of its old shellac surface.
18)  The residue left from the scraping has now been dissolved and washed away, revealing the beauty of this wood.  This is a very special variety of mahogany.   I've seen a lot of mahogany over the years but this piano's veneers are showing signs have having an almost three dimensional character that is positively breathtaking.   I'm looking forward greatly to getting new finish on this and getting it rubbed out to see just how beautiful it will end up.  It is certainly going to be a spectacular looking instrument.  Some of the veneer on the sides of this piano has come unglued.   Happily, this has not been damaged too badly so we will be able to glue it up very successfully.  Little to no veneer is missing or damaged and the actual veneer itself is quite thick.  This will make for an excellent repair to this area.

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19)  A photo to attempt to highlight why I say the bridges are not salvageable.  You can see the upper section of the treble bridge in this photo.  The cracks are so bad that the bridge is split right in two along the leading edge of bridge pins.
20)  A photo of the bass bridge up close to reveal some of the problems with it.   Due to the direction in which the grain of the bridge cap was run, the wood has actually shredded over the years.  When the new bridge is made, I will ensure that this sort of damage won't be incurred again because I will vertically laminate the core and set a thick cap with properly oriented grain.
21)  This photo shows the wood which was used to back up the pin block.  This is partly why the pin block failed.  Lester cut corners by leaving entire voids in the core of this area.  A complete, solid layer of wood is needed to glue the pin block to in order to ensure its stability.  When I repair this area, I will inset new wood where the company had left voids to ensure that we get a better glue joint than was established when the piano was new.  The more I look at this piano and how it was made, I clearly see that Lester had very good tools and designs at their disposal.   However, they cut so many corners in carrying out the construction that the finished pieces ended up with less than a perfect reputation.  It is another indicator of how important it is to do every aspect of the job very well if you want the final product to be the best there is.  With our new, high end, restoration techniques, I should be able to make this finished piano rival any Steinway upright of the same vintage.

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22)  This photo shows another reason for some of the problems they encountered.  The back beams are usually bound to each other with a thick layer of wood.  Instead, they used a thin layer of poplar (visible because it was so well protected over the years that its original green cast was never oxidized away) to attempt to bind these together.  Then a cover board with a cosmetic beauty but no structural function was lightly screwed over the back of this.  When reassembling this piano, I intend to heavily glue in a backer board which is more in line with proper high end construction techniques.
23)  It is time to remove the sound board.  However, this board is so badly cracked, I decided it might come out cleaner if I took the time to tape up some of the worst cracks before I removed it.
24)  Once the sound board was out, it became obvious that the pin block and all the spacer blocks were unglued as well.  I light tap with a hammer and chisel saw each spacer drop right out of the piano.  The pin block was so loose, of course, that it lifted out without any need of a hammer or chisel. 

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25)  Once the spacer blocks were out, it became obvious that each separate piece of maple that was glued up to form them was also coming unglued.   Another light tap with a hammer, sometimes using a chisel, saw each of the fall apart with ease.  Each piece was carefully indexed and indelibly marked with a marking punch set.  Then the wood was put into a vat of water to soak the old glue off of them.  Once the old glue was softened, it was scraped clean from the wood.
26)  In this shot, you see water soaked paper towels wrapped around the glue joint areas of the support posts and the back and side glue joints of the pin block.  Once the glue had softened, it was scraped clean.
27)  After the individual blocks were free of glue residue, a test fit was made to see how they would glue back together.  Sadly, there was enough slight warpage and such that the joints would not have been perfect.  Therefore, each individual block of maple was taken and jointed.  Then, the spacers were glued back together using the square clamped to the bench as a guide to keeping them aligned as perfectly as possible.   Despite my best efforts, however, the side and face gluing surfaces were not good enough to hold the pressure of a strung piano after I finished gluing them up.   Therefore, all the reglued spacer assemblies were taken and their gluing surfaces jointed and squared up.  This left the finished spacers too small to fit the piano as they originally did.  In addition, some of the wood used in these spacers was obviously scab wood which should not have been used at all.  Lester actually faced the spacers in such a way that the ones containing maple pieces which were too small were mated to the pin block.  This meant that the pin block was not getting glued to solid maple over 100% of its surface.  I was able to remedy this problem.  Because I had to add additional wood to the spacers in order to get them to the correct dimensions again, I decided to spin them around so that the surfaces which contained good maple over 100% of the surface faced the pin block.  See photo #30 for how this process went from here.

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28)  Soaked paper towels are laid over the areas of the piano which held the glue joint with the sound board.  This area is called the "rastin."  Once the glue had softened, it was scraped clean.
29)  Drilling out the dowel rods which passed through the ribs into the bridges.   This will make it possible for me to chisel the bridges free from the sound board.   Having the bridges free will make the construction of the clamping cauls for the new bridges easier.
30)  This shows the maple spacer blocks being glued to another board.  Once the glue dried, the spacers were cut apart into their individual pieces again.

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31)  While the glue set up on the spacers, the next step was to cut the recesses into the pin block to receive the new delignit material that will surround the new tuning pins.  Before this, I had chosen to run the pin block lightly through the planer because the time it spent under stress and unglued had caused it to warp slightly.  This planing operation trued up its rear glue joint so that it will close under lighter clamping pressure.  It is best to not need to clamp things too tightly to get the joint to close otherwise the joint could open up again in the future.   In this photo, the bulk of the material to be removed from the old pin block is being taken out at the drill press using a forstner bit.  All the holes in the maple of this are makes the removal of the wood with the router alone very hard on the router's bearings.  I prefer to remove the bulk of it this way to spare the router.
32)  Special patterns are custom made to fit this piano.  These patterns will guide the router as it finished cutting the recess in the pin block and as the mating patterns are used to cut out the shape of the delignit inserts that will replace the old wood.  This method makes for the closest fit possible.
33)  The glue has dried on the spacers and they have been cut apart.  Now another piece of wood is being glued to one edge of the spacers.  Both layers of new wood couldn't be glued to the spacers at the same time due to the number of clamps needed to seat the wood properly.  There was not enough room to install all the needed clamps all at the same time.

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34)  The finished spacers are ready to be glued into the piano.  Because the shape of the piano is not square in this area, special planing cauls had to be built and installed onto each spacer.  This allowed me to run each spacer through the planer in such a way as to get a tapered surface.  The top spacer is photographed from the side to reveal this tapered effect given to the new wood that was glued to it.  In addition, all the spacers were dry fitted into the piano so that the glue joints could be checked.  Each place that there was an inconsistency in the way the piano's back posts were shaped, that spacer had to be removed and hand planed so that it was a perfect fit.  All the time these spacers were being fitted, I had to watch carefully to ensure that I ended up with a total width for the piano which matched the original width as measured using the original pin block.
35)  Gluing the spacers back into the piano.  With the way these spacers have been reglued and repaired, the finished glue up will have better strength than it had when it was new.
36)  The glue up as seen from the front of the piano.

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37)  Now that the top end of the piano has been reglued, it's time to pull the bottom end apart and reglue it as well.  All the glue joints on this end have failed as well.  In this photo, all the rastin board, binder boards and spacer blocks have been removed and the old glue is being soaked off the beams.
38)  The original rastin board was in very poor condition.  Exposure to moisture over the years had left it soft and easily broken.  A new maple board was made to replace it, you can see the new board shows next to the original in this photo.
39)  The original oak binder board which supported the rastin partially as well as assisting in binding the assembly of the posts and spacers was in terrible condition as well.  It had become brittle and nasty.  A new maple replacement was made and is picture along side the original in this photo.

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40)  Gluing all the parts of the bottom support structure back into place.
41)  The side veneer had also come loose in places (especially near the bottom of the piano.)  While the piano was upside down, I took that opportunity to reglue all that veneer.
42)  The new pin block inserts are temporarily set into place and the plate is positioned over them now that the entire back frame of the piano is solid once again.   The plate had all its old rotten plate bushings removed and then the plate was used to mark the locations for all the tuning pins onto the pin block inserts.  This will enable me to drill the pin block out at the bench before gluing the inserts into place permanently.  Bench drilling is preferred because it is better controlled and more accurate.

View the rest of the project next year.  The customer has requested that we delay the completion of the project for personal reasons.

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