Rodgers' Piano Restorations
The Best Piano Rebuilding in the Business
9091 Ox Bow Rd.   North East, PA 16428
Because  I have a great deal of work to do, I am forced to concentrate my efforts on all matters which concern the tasks before me.   Sadly, the telephone has become a constant source of interruptions to the work schedule which consist largely of people seeking free information and telemarketers.   I lose between one and two hours each day to these people when I answer the phone.   Because of this, I have been forced to shut off phone communication so that I can better serve my customers.  In addition, the email spammers have become so thick that I am getting thousands of spams per day.  They are so thick that even spam busting software cannot stop them.  The spam has flooded my email so badly that I can no longer gain access to my own email.  Even after trying a change to the email address, the spammers found us again in a very short time.  Each time I try to access my email I simply get "timed out" because of all the junk that is in the folder.   Although I would love to be able to communicate via email, I have been totally blocked from that venue by these parasites.  If you wish to communicate with me, the best method at this time is to send a letter to the address listed above.  I know this seems slow compared to other rebuilders, but it will be well worth the effort since the quality available here is of the highest order.



Restoration of a Fischer Ampico grand for Jim Durfee

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148)  The wind motor before work began on it.   Measurement of the cloth that had been put on this motor revealed that the last person to rebuild it didn't know what they were doing.  It was covered with the same thickness of cloth that is used on the stack pneumatics.  This is too thin for the work of a wind motor.  This is done by some to try to make the motor run more smoothly.  However, by rebuilding the motor correctly, this expedient isn't needed to make the motor run smoothly.
149)  The individual components that make up the motor have been disassembled.
150)  The crank shaft and slide valves.  This motor as well as all the moving parts in the drawer had been slathered with oil.  The bushings were so soaked with it that there was no cleaning them.  Even though they weren't all that worn, they had to be replaced in order to rid ourselves of all the oil.  The rubber cloth that covers each slide valve was replaced.  Each valve was trued up by sanding on a piece of glass and then lubricated with powdered graphite.  The crank shaft was cleaned and polished and every bushing in this assembly was replaced.  Not only the crank shaft bushings but also the connecting rod bushings were replaced.

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151)  The reassembled valve/crank shaft assembly.  Not a clamp on the far end.  The mounting arm on that end had broken.  It was glued up and the crank shaft used to help it to dry in the correct position.  After the glue dried, the seam was reinforced by wrapping many layers of glue soaked thread around it.   It will never break in the same place again!
152)  Recovering the pneumatics with the correct thickness of motor cloth.   Note that the wind trunk and the surface the slide valves operate over are glued to the pneumatics in such a way that it would do great damage to remove them.  It is possible to glue the cloth onto the pneumatics without removing these blocks.  The cloth has to be carefully cut so that it doesn't overlap onto the blocks in areas where it isn't needed.  Note that this cloth has been glued to one end of the pneumatic and cut to shape before gluing to the sides.
153)  This is the automatic shut off valve and pneumatic before they were restored.

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154)  Here, I am measuring the thickness of cloth covering this pneumatic.  I suspected the thickness was, once again, incorrect.  I even checked it against an unrestored original shut off pneumatic from an Amphion that I had in storage.  I was correct about the cloth.  It was supposed to be motor cloth again.  Either the last rebuilder didn't bother to measure the original cloth and threw just anything on these or he didn't have any motor cloth and made due with the wrong stuff.  In either event, the drawer components will work better and last longer now that they have been covered in the correct material.  Note that the valve is already on its way to being rebuilt in this photo.
155)  Rehinging the pneumatic in the usual "Amphion" way of using three hinge pieces for each hinge.

156)  This wheel helps the ladder chain on the wind motor to stay taught.   The bushing on the inside was worn out and the bushing on the outside was soaked with oil.  I had to replace them both.

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157)  See the wheel back in the drawer where it belongs.   Also note that the block to the right of the wheel has also been rebushed.   This bushing had worn enough that it was too sloppy to keep.  I replaced it.   This bushing holds a shaft that transfers the turning of the wind motor over to the other side of the drawer.
158)  The wind motor governor before work began.
159)  I just had to take a picture of this!  The last person to restore this, apparently didn't know how to releather valves.  This valve is the governor bypass.  It allows a high volume of wind to pass through the governor so that the motor will run faster during rewind.  The idiot that rebuilt this, apparently was having trouble with air leaking past this valve and messing up the motor speed during play.  Instead of restoring the valve, they jammed the wind channel full of cardboard to block the air from passing through.  This solved their play problem but would have created another problem.  The wind motor would have been very slow at rewinding the rolls.  I'll be willing to wager that the owner will be tickled to see how fast his rolls rewind now that the governor is working properly.

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160)  This is an example to show that I record my mistakes as well as my triumphs.  I had forgotten how the pouch block that operates the governor bypass valve was secured into the governor.  It is held in place with two screws which are buried in felt, shellac and a metal screen on the opposite side of the governor.   I was thinking that the block was glued into place.  I attempted to remove it with a knife and a chisel.  The result was that I broke the pouch block.  Rather than attempt to glue this block back together, I made a totally new one out of maple just like the original.  I could never have trusted the original to hold its shape and stay air tight if I had attempted to glue it back together.
161)  The white square is the pouch block back in its position in the governor.  Note that the governor has also had the tempo slide valve releathered, the tempo plate and friction surfaces lubricated, the pneumatic cloth replaced and the gasket replaced with leather instead of cork.  The wire that extends out the front of the governor is the connector that controls the music tempo.  As you adjust the tempo from the drawer, this wire moves the slide valve in and out to let more or less air pass through the tempo plate.  This wire is usually bushed with felt.  The felt bushings work fine but have a minor flaw.  They let a little air leak by.   Rather than allow this leakage, I replace these felt bushings with a coarse suede leather.  It works the same as the felt in terms of letting the wire move in and out but it doesn't let any air sneak by.  Also note that the leather covering the square pouch mentioned before is white.  Normally pouch leather is brown.  This is a slightly stiffer pouch leather that is chrome tanned.  It is a little tougher than the brown pouch leather and also slightly less expensive.  It works well on large pouches and on small pneumatics.  It is a fine choice for this pouch because of its size.  If you try to use chrome tanned pouch leather to make small pouches, you will find that you can't get the system to operate at lower suction levels which is why I never use it anywhere else in these systems.
162)  This is the tracking device which has a valve block attached to it which controls play/rewind.  Again, it was covered with the wrong thickness of cloth.   In fact, the cloth had already been repaired with a pouch leather patch because it had failed so quickly because it was too thin.  The tracker is a very delicately balanced device.  If the cloth is not perfectly air tight, the thing won't work right.  It is a very difficult pneumatic to recover and, at the same time, is the one pneumatic where any leakage whatsoever cannot be tolerated.

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163)  Restoring the play/rewind valve block.  I'm always amazed at how many individual parts are created even when taking apart the smallest and simplest of player piano devices.  These systems are really very complex with tens of thousands of individual parts, each of which is vital to the functionality of the whole.
164)  Putting the play/rewind back together.  Note that all the gaskets and all other perishable components have been replaced.
165)  This is another control valve and a cutoff pouch from the drawer.

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166)  Replacing the pouch inside the cutoff block.   Originally, these got a pouch as well as a cork gasket.  The gasket is not needed provided you cover the entire board with pouch leather when replacing the pouch.   In fact, this device is more likely to stay air tight without an additional gasket.   The pouch leather works as the gasket.
167)  The tracker and play/rewind valve are done.
168)  Rebuilding the other control valves.

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169)  The play/rewind pneumatic before work began.  Once again, the cloth covering this was wrong and was leaking even though the age of it was clearly not that old.
170)  This is the trickiest pneumatic to recover in the entire Ampico unit.  In fact, this photo shows that I wasn't thinking.  I started out gluing the hinge end of the pneumatic down first.  I had to pull this apart and start over, turning the unit 180 degrees,.
171)  The restored play/rewind pneumatic.

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172)  The rights side of the drawer all restored.
173)  The left side.  All that remains is to refinish the cover boards and hardware and polish the brass tracker bar and the drawer will be done.
174)  Two sets of dampers.  One to the Bush & Lane/Welte that I'm working on and the set to this piano before work began on them.

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175)  Preparing to rebush the damper guide rails.
176)  Cleaning off the old felt and glue residue from the damper heads and polishing the damper wires.  These wires are bare brass so they also received a coat of lacquer to prevent them from tarnishing.  Usually these wires are nickel plated to prevent tarnish but this set wasn't. 
177)  The restored damper guide rails.

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178)  Rebushing the keys.
179)  The ivory keytops had failing glue joints.  They were holding on and looked OK when the piano was picked up.  However, during the storage of the piano while it awaited restoration, the joints finally failed and much of the ivory fell off.   The pieces were carefully located so that they were back on the same keys they fell off of and all the pieces that hadn't fallen off but were weak were removed.  Then the pieces were glued back into place using hide glue that was colored with titanium dioxide and clamped with pieces of glass to ensure they would be very flat.  The freshly glued ivory was allowed to sit in the clamps over night to ensure that the moisture of the glue was completely gone before removal of the clamps.  If the clamps were removed too soon, the moisture in the glue could have warped the ivories slightly and left us with an untidy finished appearance.

180)  The restored keyboard.  A few months after this photo was taken, it was discovered that the few ivories that I had not reglued had also, now, come loose.   It would appear from the condition of the ivories as well as the veneer, pin block and legs that the front of this piano must have been subjected to many decades of moderately high moisture.  The glue has suffered from this exposure.  More ivory restoration was followed up after this photo was taken to catch those pieces that showed their "true" colors later on.