Rodgers' Piano Restorations
The Best Piano Rebuilding in the Business
9091 Ox Bow Rd.   North East, PA 16428
Because  I have a great deal of work to do, I am forced to concentrate my efforts on all matters which concern the tasks before me.   Sadly, the telephone has become a constant source of interruptions to the work schedule which consist largely of people seeking free information and telemarketers.   I lose between one and two hours each day to these people when I answer the phone.   Because of this, I have been forced to shut off phone communication so that I can better serve my customers.  In addition, the email spammers have become so thick that I am getting thousands of spams per day.  They are so thick that even spam busting software cannot stop them.  The spam has flooded my email so badly that I can no longer gain access to my own email.  Even after trying a change to the email address, the spammers found us again in a very short time.  Each time I try to access my email I simply get "timed out" because of all the junk that is in the folder.   Although I would love to be able to communicate via email, I have been totally blocked from that venue by these parasites.  If you wish to communicate with me, the best method at this time is to send a letter to the address listed above.  I know this seems slow compared to other rebuilders, but it will be well worth the effort since the quality available here is of the highest order.



Restoration of a Fischer Ampico grand for Jim Durfee

Home Up Page One Page Two Page Three Page Four Page Five Page Six Page Seven Page Eight Page Nine Letter of Recommendation

235) FEAmpico235.jpg (52390 bytes) 236) FEAmpico236.jpg (19026 bytes) 237) FEAmpico237.jpg (29849 bytes)

235)  All the capstans have been relocated.  This, sadly was not the end of the story.  As I began to assemble the action and work out the regulation with the relocated capstans, I realized that there was a general error in the design of the Fischer action that I was actually perpetuating.  The Fischer specification for key travel is 1/32" deeper than standard.  With the capstan locations I chose, I was making this problem continue.  Also, I found that I simply wasn't getting sufficient hammer travel to get the kind of power I wanted out of this action.  In addition, my key weights were coming out much lower than my testing had predicted.  The action would have been light as a feather; too light.  The bottom line is that I had to move the capstans again.  The new location enabled me to do several very nice things for this piano.  I brought the key dip to a standard 3/8" like all other pianos and I was able to increase the hammer blow distance to that of a concert grand's.  The down side is that I lost about a week of extra labor working on redesigning this action; moving the capstans, moving the whippen, hammer and let off rails, etc.  This was all labor that I did not get paid a penny for.   The important thing was that the finished piano was right.  That is always first and foremost my main goal with each project.  If I have to lose money to do that, I'll do so in order to make everything right.
236)  The location of the whippen heels were what started me on the idea of relocating the capstans in the first place.  The heels did not line up with the original capstan location.  The first relocation lined them up beautifully but perpetuated a number of problems in the regulation.  It became necessary to discard my desire to leave the whippens unmolested.  I finally chose to remove the heels and move them back further on the capstan.  The bottom line is that the action dynamics of this piano were very strange to begin with and it took heroic steps to bring it into a correct alignment and function.
237)  Here, I am reweighing the action.  A brass weight which represents the amount of down weight I wish for that key is placed on the end of the key stick.   Then, lead weights are laid on the key and spaced to ensure that the structure of the key will not be harmed.  When one solid blow to the action rail to break friction will cause the hammer to rise to the point of let off, then I know I have the right amount of lead in the right places for that key.  Those locations and lead sizes are then marked on the side of the key.  Later, the key will be drilled out to accept the lead and the lead is inserted and struck to spread it out into the hole and lock it into position.  For the most part, I try to use a heavier lead that is made somewhat shallow.  These leads enable me to use a hole that doesn't go clear through the key thus helping me to retain the key's structural integrity.  A normal weigh for any piano is 50 grams of down weight in the bass tapered off to 48 grams in the treble.   However, this action did not want to give up easily.  I could not get enough up weight in the bass if I set it for 50 grams of down weight.  I must have at least 30 grams of up weight or the repetition will suffer.  Up weight is defined as the amount of weight the key can lift from the depressed position to the rest position.   In order to ensure at least 30 grams of up weight in the bass, I had to set the down weight to 55 grams.  I was still able to taper the down weight off to 48 grams in the treble.  The net result should be an action which feels fairly normal but with a solid, somewhat heavy feeling bass. 

238) FEAmpico238.jpg (55387 bytes) 239) FEAmpico239.jpg (43080 bytes) 240) FEAmpico240.jpg (41261 bytes)

238)  The player mechanism uses a hammer lift rail as one technique of controlling the volume of the music.  Sadly, the hammer lift rail installed by Fischer was entirely too flimsy for the job.  It flexed so badly that the tenor and bass hammers were all the way up to their soft play position before the treble hammers even began to move.  I was aware of this from the first moment I pulled the action from the piano.  I knew that a new rail would have to be constructed.  It was an extremely difficult and challenging task.  The way in which the lift rail was mounted to the action could not be changed even though it was not to my liking.  Any change to it was impossible because of other design aspects which had to take priority.  I had already had to move the whippen rail, hammer rail and let off rails from their original orientation in order to correct this action's poor dynamics.  I couldn't sacrifice any of these changes in order to better mount the hammer lift rail.  Therefore, the original pivot arms and mounting flanges were used.   However, I made a new quarter sawn maple rail that was glued together in two pieces designed to reinforce and stiffen the rail.  In addition, to make the whole thing work, I had to file away parts of the backs of the whippens where some spare wood on the whippens was causing the rail to hang up.  Once the rail was working perfectly, I relocated the original hammer rest felts onto the new rail.  This felt already had compressed areas in it where the hammers hit the rail.  By lining up this felt carefully, I was able to replace the felt onto the new rail directly under each shank as before.  This will help to stabilize the action regulation quicker as it pertains to the hammer lift rail.  The new rail is strong enough to lift the entire set of hammers at once and in perfect line.  It was a huge undertaking to make this rail anew but well worth the results.  The old rail would have seriously compromised the quality of the reproduced music.  In fact, that rail had been compromising the music since the day it left the factory!  Another item you can note in this photo is that I had to add additional felt to the drop screw locations in order to correct a clearance issue with the drop screws.  This action was built with the rails so misaligned that the new parts couldn't engage the drop without adding thicker felt over the tops of the whippens drop screw contact area.
239)  The various parts of the player mechanism have been reinstalled into the piano.
240)  All the tubing is now in place.  You will note a white piece of wood running down the pneumatic stack cover which contains four snaps.  The original board that the vinyl action cover snapped to was missing.  In fact, the entire back cover had been replaced at some point in time and the person who replaced it neglected to install this board.  I used a piece of poplar to make a new rail.  Happily, I had the old cover in my possession so I could use it to locate the snaps exactly where they used to be.  Since the cover will completely hide this board, I didn't paint it.   Actually, I had run out of black paint as well but this was fine since the cover would totally conceal it anyway.

241) FEAmpico241.jpg (34840 bytes) 242) FEAmpico242.jpg (31095 bytes) 243) FEAmpico243.jpg (35573 bytes)

241)  The new cover has been made and installed.  Many rebuilders use the original covers as patterns to make the new ones.  I did have the old cover and could have done so.  However, I am able to make a much better fitting cover if I don't bother using the original as a pattern.  By a technique I have developed, I get a perfectly fitted and taughtly stretched cover just by using the piano itself as a guide.  You'll also notice that the tubing that passes from the drawer into the spider over the pneumatic stack has been covered with vinyl as well.  This early piano did not originally have these tubes covered.  However, Ampico mechanisms had this feature added to them by the time they had switched away from using the poppet stacks.  I feel this is a very nice improvement that they made.  Since it is an authentic thing to do because the factory did eventually come around to this idea as well, I felt that I could safely improve this piano by adding it to the design even though it didn't have it originally.  To do this, the male ends of the snaps are screwed onto the drawer and the stack cover in the places that the factory chose to place them later.   The vinyl is then fitted over the tubing in such a manner that it conceals all the tubing (even the lead tubing at the back of the drawer) without interfering with the sliding motion of the drawer in any way whatsoever.  Another item you will note are the snaps.  It is customary to use black snaps to make these covers.  However, I couldn't find enough black snaps in the entire city to do the job.  I had to resort to nickel plated snaps which actually look very sharp even if they aren't exactly what was used originally.  One other item to note are the screws which hold the wooden stack covers in place.  These can be very confusing since it is hard to tell which screws hold the covers together and which screws hold the assembly to the stack.  I use a nice little trick to help my customers in the future.  I replace the black headed screws with nickel plated screws everywhere that a screw is needed to hold the cover to the piano.  If you need to remove the front cover or the back cover, just take out all the nickel screws and leave the black screws alone and it will come right off.
242)  Behind the green cloth at the back of the key in this photo are hiding the tops of the poppets which activate the keys.  While the piano was still on its side, I took the action apart and installed the key frame.  I clamped the frame down so it was seated on the key bed.  Then I placed the keys onto the frame one at a time and checked the clearance between the key and the poppet by looking around the drawer at the pneumatic on the other side.  If tapping the key moved the pneumatic, the poppet was too high.  If the pneumatic could be moved more than a very small amount without touching the key, the poppet was too low.  The wooden head of each poppet is screwed down over the threaded wire that connects it to the pneumatic.  These wooden heads are then screwed up or down as needed.  The only down side to this system is that the wooden dowels are extremely difficult to turn if the metal has corroded even a little bit.   These were bad enough that I had to be very careful not to break any of the wooden lifter fingers which these wires sit in on the pneumatic.  Also, the job of turning these was so hard on my fingers that, by the end of the day, the two fingers I was using to do the work were swollen so badly they felt like they were going to pop right open!!  
243)  The restringing on the piano is complete.  Now it is time to install the damper system.

244) FEAmpico244.jpg (23092 bytes) 245) FEAmpico245.jpg (47267 bytes) 246) FEAmpico246.jpg (36305 bytes)

244)  The upper part of the bass section of this piano was designed with wound trichords.  These are notoriously hard to damp.  To solve the problem of good damping, I have added extra weights inside the damper heads as shown in this photo.  I also had to spend about half a day trying different damper felt types and positions until I found the best one to damp these strings.
245)  Testing the finished piano.  These systems always have problems when you first fire them up.  The job is to work with the system until the player mechanism is working perfectly in every way.  Once all the bugs are worked out, the piano will be allowed to continue to play for many hours and through many different rolls.  The goal is to confirm that the piano will operate faultlessly for the owner.  In this photo, you can see that pressure readings from both sides of the stack are being taken as the piano is playing.
246)  The finished and reassembled piano.  Now that it has had at least 20 hours of playing time, I will go through the entire action, damper system, pedals and poppet rail and reregulate everything.  I will also tune the piano again.  Now that the action has been played in, there is a good chance that these settings will stay put for a reasonable period of time. 

247) FEAmpico247.jpg (41228 bytes)

247)  The owner poses with his piano after delivery.