Rodgers' Piano Restorations
The Best Piano Rebuilding in the Business
9091 Ox Bow Rd.   North East, PA 16428
Because  I have a great deal of work to do, I am forced to concentrate my efforts on all matters which concern the tasks before me.   Sadly, the telephone has become a constant source of interruptions to the work schedule which consist largely of people seeking free information and telemarketers.   I lose between one and two hours each day to these people when I answer the phone.   Because of this, I have been forced to shut off phone communication so that I can better serve my customers.  In addition, the email spammers have become so thick that I am getting thousands of spams per day.  They are so thick that even spam busting software cannot stop them.  The spam has flooded my email so badly that I can no longer gain access to my own email.  Even after trying a change to the email address, the spammers found us again in a very short time.  Each time I try to access my email I simply get "timed out" because of all the junk that is in the folder.   Although I would love to be able to communicate via email, I have been totally blocked from that venue by these parasites.  If you wish to communicate with me, the best method at this time is to send a letter to the address listed above.  I know this seems slow compared to other rebuilders, but it will be well worth the effort since the quality available here is of the highest order.

 

Restoration of a player piano that is also an orchestrian for the Dahl family of McKinney Texas

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67)  The pin block is now finished.  The inserts have been glued into place and all the holes where the plate screws go into the piano have been plugged with new Delignit pin block material plugs.  The original screw holes were stripping out.  You can also see in this picture that the upper treble bridge cap is not on the bridge.  The outer layer of wood on the bridge, known as the cap, fell off the bridge after the bridge pins were removed.  To ensure the best possible tone in the treble and a long lasting quality, it was decided that this cap should be remade rather than just gluing the old one back on.  This job will be done at no additional cost to the customer.  The reason for doing it is strictly because I don't want a piano leaving my shop with a bridge cap that is in that bad a condition.  Some of the cracks in this cap go quite deep and would be difficult to repair.  Therefore, it will be replaced.
68)  After the sound board was dried sufficiently to reveal all cracking that was likely to occur, a total of 25 feet worth of cracks were discovered.  Here, you can see the die grinder with the special router bit and guide that is used to clean old wood out from around all cracks.  The new spruce shims that will be driven into these new voids are made to match the shape and size of the cutter exactly.
69)  This picture was taken after all but one of the cracks had been prepared for shims.  The final crack could not be done at this time because both panels of spruce that it was adjacent to were totally loose from the sound board.  It was, therefore, necessary to do all of the regluing before this final crack could be cut open for shimming.  In fact, all of the cracks that were below the long bridge also showed very bad glue failure between the skin of the board and the ribs.  However, the rest of the glue joints were sufficient to hold the skin safely in place while it was routed for shims.  All except this last one.  When it was time to plan the screw locations for regluing the skin to the ribs, the skin of the board was pressed firmly from behind so that any glue joints that were holding but weak would let go so they could be repaired.

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70)  This picture shows that the skin of the sound board has been reglued.   Before any regluing was done, wedges were driven between the sound board and the back support posts.  These wedges force the sound board into the crowned shape that it was originally designed with.  By installing these wedges, it is possible for the new shims and glue joints to take on this crowned shape permanently, thus giving the board back a degree of its original strength and vibrancy.  The clamping pressure is exerted using screws with washers under them to keep them from digging into the sound board.  Even the areas that were not coming unglued from the ribs were reinforced with dowel inserts.  To the left of the long bridge in this picture, you can see that holes have been drilled into each intersection of a rib and a crack.  Dowels will be inserted here to discourage the currently solid glue joints from coming apart in the future.  If it had been in the budget to do so, it would have been immensely preferable to replace this sound board.  Never before have I reglued a board that had gone this bad.  However, it would have required an additional $3500 to replace this sound board.
71)  After the glue had dried, the screws were removed and all the screw holes were drilled again to make them the exact size necessary to hold dowels tightly.  These dowels will reinforce the joint and discourage it from failing again in the future.   In this picture, you can see that the dowels that go above and to the left of the long bridge have already been installed.  The dowels that will be going below and to the right of the long bridge have all been dry fitted and sized for length, then they were placed partially in their corresponding holes.  Next, each dowel was picked up, coated with hide glue and driven into place.  Because of the way this board had to be restored and because of the hard life it has lived, it is impossible to make the back side of the board look good but the front side will be well sanded and steps taken to make it look as close to new as possible.  There were so many places that had to have dowels that the thinner areas of the ribs had to be drilled clear through so that the dowel inserts would have the maximum amount of rib to grab ahold of.  This is one reason why the back of the board will not be able to be made to look as good as one could hope.
72)  All the 25 feet of new spruce shims have been fitted and driven into place.   In some areas, it was necessary to place the shims under clamping pressure to keep them tightly in place until the glue could set up.  Because the shims are straight and the sound board has been wedged into a crowned shape, the longer shims don't always stay tight in the joints just by the driving pressure that was exerted while installing them.  If a shim tends to pop up a bit, a clamp is put on it until the glue can set.

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73)  The sound board shims are being trimmed flush with the surface of the sound board.
74)  A view of the new sound board shims seen from the back of the piano.
75)  The sound board has been scraped clean of its old finish.

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76)  Now we're ready to make the new bridge caps.  This is a picture of the bass bridge which was removed from the sound board to make room to for shimming work.  You can see from this photo that the last "rebuilder" had this cap fall of on him/her.  This person glued the cap back on using screws to clamp it down.  The screws were not sufficient for clamping since, as you can see, they did not allow the edges to become secure.  In addition, the cap was misaligned during the regluing process.  You can see this misalignment in the photo.
77)  This picture shows the one section of the bridge caps that is being reused.   It is being renotched.  However, because the wood was a bit soft, it didn't respond well to the chisel.  Therefore, the die grinder was used to restore the points on the bridges where the strings meet the bridge.  This must be done so that the strings will have the best possible tone.  If the notches on the bridges are not very clean and in perfect alignment with the bridge pins, the strings will be false.   That means that one string will sound like two strings that are out of tune with each other.
78)  Duplicating the treble bridge cap.

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79)  Gluing the treble bridge cap into place.
80)  Gluing the new bass bridge cap onto the bass bridge core which has already been removed from the piano to make way for the shimming operation.
81)  Transferring the pinning pattern onto the new bass bridge cap.

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82)  Drilling the bass bridge to receive the new bridge pins.

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